Exhaust Elbow Blues, Reprise

Raise your hand if you thought we would have some trouble with that exhaust set up on Galapagos during our recent shake down trip from Astoria, Oregon to Tacoma.  Yeah, don’t gloat. Because our hands are raised, too.  If you’ve been following the Drama of the Exhaust System, you’ll recall that we had a fancy new engine exhaust pipe made to fit the boat because we were worried that water would back up into the engine, drowning Hiram and making us dead sad. If you are new to this series, read about that here and here to catch up with the rest of us.

The new pipe fit like it was made for Galapagos because, duh, it WAS made for Galapagos to the tune of (Put coffee mug down here) an amount of money that is very large.  When you pay several hundred dollars for a specially machined piece, you kind of think things would be right but that’s where you would be wrong.

Freshly installed and wrapped. This tape turned out to be really good.

From the get go, Mike was concerned about the weld holding the new piece of metal pipe to the flange that was used to attach the thing to the Beta. It just didn’t seem that the piece had enough support to keep that particular joint intact but the mechanic who fashioned the piece assured us that it would be fine. We wanted to believe him because we really were anxious to turn the page on that chapter of the refit. The pipe was pretty. It fit nicely. The kid who made it was a nice kid. Hiram hummed along perfectly well. Mike added rubber washers to the support on the right, wrapped the thing in insulating tape, and vowed to keep his critical eye on it. We figured it would eventually be a problem but we wanted to get going bringing Galapagos up to Tacoma. What could possibly go wrong?

All was well until we were anchored in Bellingham Bay ready to visit our son Andrew for a couple of days. Mike had been doing his usual checks in the engine room and I could tell by the cut of his jib something was amiss. Then the cursing began. It’s always quiet, but it sounds even worse that way and after the time he found water in our new engine’s oil, whenever I hear silent cursing coming from the engine room, I have a post traumatic experience. He found that the weld had separated just where he’d been concerned it would, and what was holding the pipe together was the insulating tape. And because of  the leak, the exhaust gases were now allowing water to make its way back toward the engine! Oy. When we examined the broken weld, we saw that the piece had been butt-welded, not beveled or supported in any way. Sheesh. Do we need to learn to weld in order to see that things are done right?

You can see the complete break in the middle of the photo. Ouch.

You can see the complete break in the middle of the photo. Ouch.

He removed the tape, which was black on the inside from engine exhaust. The pipe was in two separate pieces. Mike attempted a temporary fix using high temperature silicon tape but the gas pressure made that fix very temporary. There was nothing for it but to get the thing repaired. I held my breath as he checked the engine oil. No water. Praise the powers that be. Hiram was safe. Another bullet dodged; another withdrawal from the Kitty of Karma. We better start making some deposits there.

These are the times that try the souls of boat owners and we feel extremely lucky that this happened in Bellingham when we were safely anchored and had access to a car and services.  Really, life was incredibly good just then and no stinking exhaust pipe was going to ruin our time. Mike thought we might be stuck in Bellingham with the exhaust system blues for a few days. I can think of worse places to be. Andrew rescued us with his car and he and Mike carefully rowed the piece to shore. 

Mike took the piece to a place he had called (thank you, Iphone), and they referred him to someone else, etc. By the following day he had located Chad Peterson of Peterson’s Welding and Fabrication.  After consulting with Chad (our new best friend)  we left the parts with him and spent our waiting time purchasing aluminum stock and doing some other fun things we’ll write about later. It was a good day, one that made us look forward to being retired and having time to just go with the flow.

Mike planned to use the aluminum stock to make new support struts and called our loyal mechanic, Shawn, who had also been a little concerned with the exhaust pipe installation. Thankfully he is very responsive at picking up the phone when Mike calls. You’d think he’d be tired of hearing from us by now. He had some good ideas to add to Mike’s good ideas and a plan was formed.

Shawn maintained that the pipe needed to vibrate in time with the engine vibration and therefore needed to be supported by struts that were attached to the engine. That made sense to us. Hell, what do we know?  So in addition to beveling and welding the pipe, Michael asked Chad to add a cross brace with holes in it to create a more stable geometric form that would also provide landing points for the new support struts. That way the pipe and the engine could both sing the same song.

In deep mano a mano consultation with Chad. The amount of testosterone in this workshop was mind boggling. I had to get some fresh air.

A few hours later we picked up the newly welded piece. This time the two parts were beveled to allow a greater amount of surface area to be welded. We can only hope. It all looked great (just like it did last time… just saying) so we paid Chad less than I thought it would be and returned to the boat. These kinds of things are why I still work.

Mike tests the tensile strength of the finished piece. He is pleased.

Installed and ready for new supports. There is so much more structural integrity just with the crosspiece added. Geometry, people. Geometry. Live and learn.

Back at the man cave aboard Galapagos Mike created two support struts for this piece of metal art we call an exhaust ‘elbow’ and found places to attach them to the engine. We had picked up some aluminum flat and angled stock while waiting for Chad to work his magic. Without shore power, Mike was limited in how much actual cutting and drilling he could do to build the struts and aluminum is much easier to work with than steel. He also decided that he would leave the insulating tape for later so he could keep a close eye on the thing. A very close eye.

We left that afternoon and spent a lovely evening at little Eliza Island, just an hour from Bellingham. Everything was holding thus far. We know this because every time I looked up Mike had his head in that engine room, gimlet eye focused narrowly on Hiram’s elbow.

Two supports. He may put in a third one but this is it for now.

Two supports. Notice one is a flat piece and one is an angled piece. There will be a test on this information later.

The following day we had a long motorboat ride with some minor sailing down Rosario Strait. The pipe had plenty of opportunity to break if it was going to do so right away. All went well and we pulled into Griffon Bay to spend the evening, planning to cross the strait the following day.

I’d like to say that this was the end of the story, but alas, our karma doesn’t work like that in this instance. This sentence is what is known, in literary terms as ‘foreshadowing’, a term which, as used here, means ‘giving a broad hint about things to come’.

We had a lovely sail across the strait the next morning, ending up amazed at how much distance this boat can travel in a day compared to Moonrise and how it can do 12 knots around Wilson Point and never even think about surfing. Speed demons!  We motored some, but sailed more and still had record speed in the crossing, for us. We made it to the south end of Whidbey Island before anchoring for the night in the currents of Useless Bay.

Anchored in Useless Bay.

We had more sailing on the final leg of the trip. In all, we sailed a good part of this trip from Astoria to home. Even so, one of the supports turned out to be a sacrificial piece. The day after we pulled into our slip at Foss Harbor, Mike was doing his thing checking all things Hiram in the engine room. I heard that small little cursing I’m beginning to know so well. 

Oh yeah. The flat piece of stock sacrificed itself on the alter of vibration for the sins of the exhaust elbow. It took the load and the load broke its back. Pause for that moment of silence.

We have some more ideas about how to solve this problem but we want another pair of eyes to take a look so Mike will be busy finding someone in the Tacoma area who can give us another opinion. Looking at the system as it’s set up, it seems to us that on the right (in the photos) the rubber piece that connects the pipe to the water muffler serves to absorb the shock of the vibration. There is no such piece on the left, and this is too bad. Even if the thing vibrates in time with the engine, there is too much vibration for it to hold for long.

My idea was to have the thing cut into two pieces again, take part of the rigid pipe out, and insert a rubber piece on the left side. That would surely absorb the vibration on that side. Mike says that’s not an appropriate place for a piece of rubber. I believe him because, again, what do I know? But surely there is an equivalent piece in the world of metals? He says there is. So our current thinking is along those lines. At any rate, now that the engine has some hours on it (82 to be exact) Mike wants to have the alignment rechecked by yet another diesel mechanic. At that point we can discuss the elbow and see if we can somehow design a system that will let us sleep at night.

So for now, we take it easy with the engine until we can get this issue resolved, again. That’s okay. It just encourages us to raise the sails.

This makes it all worthwhile.

This makes it all worthwhile.

New Docklines: Thanks Northwest Rigging!

Melissa and I decided that a we were in need of break this weekend. Instead of schlepping down to Astoria and working non stop, we stayed home and only worked at half speed. Melissa put some time into her garden which is looking beautiful. I helped by taking a nap.

But even when we aren’t at the boat, we are thinking boaty thoughts. We are doing boaty things. Melissa has finished up a number of the cushions for the salon with a beautiful new fabric ( a future post on those is in the works). For my part, I have been making new docklines for the boat thanks to the good folks at Northwest Rigging.

Back in February, Melissa attended the Women’s Boating Seminar in Seattle. Melissa had a great time; especially when she won a $200 gift certificate from Andy Schwenk at Northwest Rigging. This was a stroke of luck for us because the docklines on S/V Nameless are so stiff that we can barely wrap them around a cleat. They are 3/4 inch three strand and are almost unworkable. We have washed them and they are a bit better but still pretty difficult to use.

I was thinking that the Brait lines made by Yale or Samson would be easier to handle and store. If you haven’t seen this line before, check out Yale Cordage’s offering. It has a very easy hand and offers good stretch and strength; similar to traditional three strand but much softer.

So a couple of weeks ago, I went up to Fisheries Supply and used the the Northwest Rigging account to buy most of 200 feet of 5/8 inch Yale Brait.

Yale Brait

New Yale Brait with an old, stiff dockline in the background

Now 200 feet seems like a lot of line. The plan is to make two 25 foot lines for the bow and stern and two 50 foot lines to act as spring lines. That will leave 40 or so feet left over which I may make into a snubber for the anchor chain.

YouTube is great for so much more than cat videos. I was able to find a couple great splicing videos (see at the bottom of this post) from Samson and Yale on braiding the 8 strand line. It is very similar to splicing three strand; there are really just four parts that you have to keep straight. Check out the photos below:

Yales’s Brait has eight strands but they are in four pairs, making the splicing fairly easy.

Tuck, Turn, Tuck, Turn

Tuck, Turn, Tuck, Turn

After seven tucks, I cut one strand and finish tucking the remaining strand until I run out of room.

After seven tucks, I cut one strand from each pair and finish tucking the remaining strand until I run out of room.

I like to splice Al Fresco

After finishing the loop and cutting the lines to length, I like to whip the ends. It gives the lines a salty look and is easier on the hand than a hard, melted glob of nylon. Although more work, I thought it would be nice to have two whippings on the 50 foot lines to make them easier to identify. Again, thanks to YouTube, I learned to make a whiplock after whipping the line and really like the way it looks. Hopefully it will make the whippings last longer too.

The double whipped 50 foot line on the left.

I’ll finish the docklines this weekend and save the remaining brait for the snubber. If you have never tried splicing your own lines, check out the videos below and give it a try. You’ll enjoy handling the lines all the more knowing you made them yourself.

This is Samson Rope’s video on Brait Splicing. The video a little tedious but thorough. You can adapt the lesson learned to other sizes and brands of cordage[vsw id=”-zUFloSvYLk” source=”youtube” width=”425″ height=”344″ autoplay=”no”]

This is an Annapolis Performance Sailing video on locking the whip stitch.[vsw id=”9RY2WZivFS0″ source=”youtube” width=”425″ height=”344″ autoplay=”no”]

Also, take a look at Captain Mike’s quick rope whipping tutorial: http://captnmike.com/2011/10/26/mikes-quick-rope-whipping/ His site is full of useful articles on other topics, as well.

Finally one last thank you to Andy Schwenk at Northwest Rigging for supporting the women’s boating community. These new lines should help take some of the stress out of docking the boat.

 

 

 

It’s Alive!

After month’s of preparation, worry and doubt about whether we could actually pull this off, The new Beta diesel drew her first breath aboard Andromeda

[vsw id=”S8IgC02W0ik” source=”youtube” width=”425″ height=”344″ autoplay=”no”]

As you can hear,despite Shawn’s declarations, it is not exactly quiet. The control brackets are still loose and rattling and we have a few other adjustments to make. I expect we will be able to dampen the noise more as we complete the final adjustments

One adjustment that had to be made right away was to move the starboard mounting rail outboard a bit. The engine was hitting it and creating a loud knock

Engine rail is impinging on engine mount support. This made a lot of noise.

Shawn was able to gain some space by moving the rail outboard a bit which stopped the clanking but now we have to grind out the mounting hole to fit two of the bolts in. That will be a messy nuisance. No doubt, we will be repaint some of the engine room after the boat is back in the water.

One of the challenges to starting the engine on the hard was getting water to the engine. Without raw water, we would only have been able to run the engine for a couple of minutes (with the raw water impeller removed). For some reason this seemed like a difficult problem as the only available water is some distance away at the travel lift. In the end, the problem was easily solved with a run to the hardware store for an extra water hose which allowed me to extend the existing hoses to our boat. Using a five gallon bucket, we were able to create a fairly flexible cooling system.

Our ersatz raw water system

This coming weekend I will install the control cables and, hopefully the steering system. If Shawn can open up the holes on the engine rails, and re-install the mounting bolts, the engine will be done until we are back in the water and ready for our final alignment.

I am also happy to report that the fuel system I installed worked beautifully and, amazingly, no leaks. Shawn had suggested that  I install a valve on the return line so that I could vent fuel into a container when priming the engine. I did that and added a switch into the system which allows me to run the fuel pump from the engine room to aid in filling the filters and priming the engine. Everything works well and the fuel looks good.

And Shawn made progress repairing the fiberglass. I really appreciated seeing how he approached this repair. Take a look.

After saturating the area with resin, Shawn stuffed long strands of glass around the the roughed up area. The green stuff is last week’s Kitty Hair.

Shawn applies more resin and drives it into the glass with a resin roller.

Next comes a bit of roving. Again wetted out with resin

 

Two more layers of a somewhat finer cloth and more resin brings us to this.

Shawn completed this repair in between engine adjustments. The actual time involved in building up the fiberglass to what you see here was probably twenty minutes. Pretty amazing. I think he wants to put down one more layer of finer cloth to help in fairing the repair and then a different kind of resin to cap the whole area. After that, a bit of sanding and antifouling paint that little chore will be done. As you can see, the bronze fitting has been moved out of the way to facilitate the fiberglass repair so that will be re-installed and then the prop  will be properly seated on the shaft.

Finally, lest you think that all I do is work on this damn boat every weekend, I’ll leave you with a photo of my latest hangout in Astoria. The Rogue Public House is on the east side of town which I rarely visit, until now. The Rogue brewery is well known in the Pacific Northwest especially for the Dead Guy Ale. Well you can have that and about twenty other interesting beers, ales and stouts. This being winter, they have about five delicious stouts on tap. Awesome pub food, a no cell phone policy all in an old Bumble Bee Tuna Cannery.

Work is our Joy. Couldn’t have said it better, comrade bee.

Stay tuned. Next week, Lord willing, we will actually be able to steer the boat!